


As title really, I will let Andy fill you in on the details.




Essentially he hit 408bhp at 1.6 bar i think?



The day was severely hampered by a coolant problem which Andy has got to track down.


Excellent results though!!

Neil.

Moderators: IMOC Moderators, IMOC Committee Members
Andy F wrote:Thor are a very professional bunch, highly recomended.
Great day, now to sort this air lock, weres mi spanners???
nutter wrote:Nice figures! What i/c/ CC are you using andy?
nutter wrote:jesus! Makes me wish i'd not sold my greddy now!
jonno wrote:It was*very* cold in there today, we were both shaking with cold for most of the day
- I took shelter in the office with an electric heater!.
It is a big IC core though, much bigger than I expected and Andy's turbo is a monster so assuming the core will flow the boost, inlet temps shouldnt have been an issue today.
Proof of the pudding will be at 30 degrees at Elvington in the summer!.
nutter wrote:Nice figures! What i/c/ CC are you using andy?
MR2Mania wrote:Andy F wrote:Thor are a very professional bunch, highly recomended.
Great day, now to sort this air lock, weres mi spanners???
Andy, what did they think that the coolant problem could be? Did they say any more after we spoke on the phone?
Those are WICKED numbers! Although the graphs look a bit weird in the midrange.A bit like a set Neil had done there.
Why does torque dip at about 5300RPM? That's roughly where it should be peaking.
Glad to hear you've finally got some good numbers though, mate!
Andy F wrote:Hi mate
They didn't really say, i now think its getting under the HG, gonna try re-torqueing the head bolts a bit more![]()
Also putting that bent pipe back on.
Pretty sure its not a cracked block cos Fraser checked for this last time(enderscope) ouch
will have a mess tomorrow, and let you know if i have any joy.