



The car is exactly as per before the turbo was removed, but I have removed the boost controller to simply the system to help try and diagnose the problem.


The boost just keep rising until it hits fuel cut at 18psi by about 5250 rpm

All pipes have been checked for leaks, the actuator has been confirmed to be operating correctly, isn't hitting the downpipe etc.


I have had the car checked over by a local Jap car specialist, and is currently back with Turbo Technics but we are all at a loss as to what the problem could be.


The car is fitted with a 3" decat downpipe and a 3" Fujitsibo exhaust which I have been running for some time without issue before the turbo rebuild.


The only current explanation is that the rebuild turbo is flowing so much more that due to the extra flow of the full 3" system it cannot control the boost.







Does anyone have any experience of running a 3" de-cat and 3" system with a freshly rebuild standard CT20B turbo?