






Well done, keep it up
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jimGTS wrote:If you cant see or hear cc water flowing, then you have some air in the system somewhere downstream.
I had a similar situation, no leaks, all hooked up fine, turns out just needed to bleed the pre rad a little more.
markstevieandmads wrote:jimGTS wrote:If you cant see or hear cc water flowing, then you have some air in the system somewhere downstream.
I had a similar situation, no leaks, all hooked up fine, turns out just needed to bleed the pre rad a little more.
Thanks JimGTS.I thought this.Im using the original st205 chargecooler rad so hoping i can reach the bleed valve on it
(if there is one).
I cant remember bleeding from there when i installed it though my memory is getting bad lol.
The pump is definitely working so i know its not a big problem.
One thing i noticed yesterday while bleeding the coolant is when i opened the throttle the coolant would come back out the open coolant cap area.Is this normal? It did settle down after a while though but i cant remember it doing that before?
thomp1983 wrote:Chin up mark it shouldn't be too hard to sort, how was the repair done last time drilled out and helicoiled? Id be looking at fitting a timesert which you can do in situ and are far more reliable
thomp1983 wrote:If that is the case then you should just be able to enlarge that hole on the manifold slightly to let it sit flush.
You need to get a bare manifold and test fit it without a gasket against the head and it should sit near flush to the head
markstevieandmads wrote:Im going to try to remove the stud and make the exhaust manifold hole bigger with it in situ(being careful not to hit the head).
Then reinstall the stud with threadlock and hopefully then wont need as much torque for it to hold?
The other option if the thread is knackered is to tap it out to 7/16 and get a 7/16 stud? Ive read this on a usa forum.
Just trying to save me the hassle of removing everything again.
rossonza wrote:markstevieandmads wrote:Im going to try to remove the stud and make the exhaust manifold hole bigger with it in situ(being careful not to hit the head).
Then reinstall the stud with threadlock and hopefully then wont need as much torque for it to hold?
The other option if the thread is knackered is to tap it out to 7/16 and get a 7/16 stud? Ive read this on a usa forum.
Just trying to save me the hassle of removing everything again.
looked at helicoils?