Hi Mate,

Yeah the car was mapped with mixed results.

We got the car on the rollers and had a play.

After setting up the AEM boost control the car was run at wastegate pressure to see what was what.

In this state at 6-7psi we made 230bhp, nice, good spool.

We then upped the boost and re-mapped at 1.0bar, even better we made 350bhp and thought this is going well.

James at 3S who was otherwise quiete curled his bottom lip and nodded.

Then we went for more boost so dialled in 1.4bar.

Now the power increase was not good.

We couldn't figure out what was up and ran out of time on the dyno as Lockys car had to come on.

So we went on the road to check things and had a big missfire.

We changed the plugs on Ryans advice to coppers and went out again.

We then discovered the stock knock sensor was throwing up a lot of random noise and causing the AEMs knock control to retard timing.

So switched off active knock off and the car started to motor, now we had too much fuel, so Ryan suspected a poor flame front on the dyno

(due to plugs?) leading to poor figures at the higher boost setting.

We trimmed fuel and managed to get in 4-6' of advance cant remember which.

At this point the car felt good and was going nice, but as the dyno was closed we got no final power figure.

So to summarise
[email protected], unknown at 1.4bar

It is very laggy for a 3071r though.

I have spoken with Ryan and he knows I am not happy about the lag, but he has offered to come to me and sort things out which is cool.

Once its on boost it flies but its so slow getting there.

Especially for my setup.

So lets see what Ryan can do on the second tune up.

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