













































And few days later bought this

























































Time came to pick her up.



Unfortunately she lost drive on the M25 after I lost the front number plate on the M11 lol







The COR was the culprit













Got her working next day after advice from Mr Brett.






With Patrick informing me of the nasty wiring I popped down to him.






Wiring tidied up nicely and ECU shifted a bit further to the left with a mk2 COR installed







Retro original cloth seats in







Air scoop off







Front bumper off and changed for an original Mk1a bumper complete with new number plate













Plan is to fit one of Patrick's Haslbeck front splitters with PW's wide arches







Also removed the red gear gaiter and knob and screwed a mk2 knob on







So on way back from Patrick's I managed to overheat her and pop a coolant hose off.




The rad fans only operate on a manual switch.



Ordered these











Thought I'd crack on with the coolant.









Started refilling and got a leak.








