


Bought on 9th Dec 2010





Nothing goes to plan and I was expecting problems, but I didn't expect anything as heart breaking as this.





The engine arrived at Woodsport and appeared to be very badly damaged and in an unsaleable condition.








There were missing parts.









Response from the Yard after my email saying that it was in an unsaleable condition.













Quick run down of the problems with pics from Paul.




Both front bank camshaft sensors broken.












One of the bellhousing bolt holes snapped clean off the engine.








The front bank cam cover had a crack on top of the casing.








Engine harness badly chopped in several places.













Missing parts included upper dipstick tube and dipstick.










The good news was that Paul could salvage it.






















I bought a rolling MR-S shell from GTSChris.








Work started with Paul Woods in Jan 2012





Alterations carried out to the engine bay, certain areas recessed and the drivers chassis engine mount fabricated.








The front subframe modified too, necessary for Marcs headers to clear.








Gearbox hanger mount made





The Mk2 mount dummy fitted on the drivers side.








The engine access hole cut and framework made for it that the removable hatch bolts to.








The large core aluminium rad fitted, essential for a 2gr or 1mz in a roadster, the stock radiator is pathetically thin.








Engine looks a lot nicer now compared to the previous pics!!





The engine bay prepped and primed.










Then given a quick basecoat of gunmetal grey.


The engine trial fitted.








This highlights any areas that need to be addressed and lets Paul make the torque mounts and modify the rear subframe.








They really are a snug fit in a Mk3 bay.








Start made on the gearbox side of the rear torque mount.








Front torque mount fabricated, pre paint.








The rear one with temporary bolts.








A view from the rear, still a bit untidy.








Fabrication stage complete, engine removed and bay given final alterations before getting a clearcoat on the basecoat.








I've lost the first fire up videos.




There was a code P2103 coming from the ECU, which means the drive by wire throttle body had a fault.


It couldn't be ignored because it goes into limp mode and restricts throttle to 2000rpm.


So another throttle body was required!

I bought a 2nd hand throttle body from ebay US.





So the ebay one was fitted, key turned.












Two codes from the ebay TB are:
P2103 Throttle actuator current


P2111 throttle actuator control system


We decided to get one of Paul's friends' 2gr into the workshop so we could cross over a known good TB and ensure the wiring is all OK.








I sourced another new TB, this time tested as working before it was sent to me.


Getting excited about picking her up, I gave her some new boots.


Rota Grid wheels in Bronze with Toyo T1-R tyres.


Front wheels:


Front tyres:

Rear wheels: 16 x 7J

Rear tyres:






I finally picked the car up from Paul on 2nd May 2012.









Dick had plenty more than a hardtop.










Stopped at a petrol station when I was on my way again and got a flat battery.








Finally got home in the wee hours of the morning.


























First jobs I carried out the following week were new battery and new tyres for the front.


